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The problem seems to be fixed now. I gooped up the bolt with sealant tightened it as much as I could and let it sit for 2 days before I put coolant back in, everything seems to be working fine. Thanks for all the replies!
Sadly the bolt is fine, the hole is stripped. I'll grab a helicoil from work tomorrow and try that. Even with the car running I still can't drive it, I can't seem to find any linkage for the tranny!
A new problem has risen!
Alright, after removing the leaky bolt, drying everthing and then applying sealant I've realized that the bolt is stripped! So, now I have to try to tap some new threads without removing the head.(yeah, like that's gonna happen)
Anyway, thanks for the replies and...
Well, I finally got my newly rebuilt 383 engine started and noticed that it was blowing a lot of white smoke. After shutting it down I noticed that there was coolant coming from the passenger side exhaust manifold. I knew that it had a crack where the nut is, but I hoped it would be alright. I...