70GS455
Member
This is a video of a dyno test of a 6322 850 cfm on a 482 BBB. Can anyone spot the obvious mistake regarding the rear air door? We were also getting fuel from the squirters that has been since resolved.
Yes. We were pulling alot of vacuum during the tests. I believe the suction was just drawing fuel past the check valve. We first put a spring on top of the check valve which stopped it but we lost the squirt function. So later I bought some CS squirters which fixed everything.Air door too open = Way too open if it has 131 jets
it shows on door! Not enough tension on Air Door
spring.
Is check valve leaking and pump squirters dribbling?
That is all I see until I can find my reading glasses?
Good eye. I eventually want to keep an operating choke but we were just testing without it.Rear door.
The small plate that covers the air bleeds is missing. The driver's side one also acts as a stop for the air valve at WOT. Removing the choke is a good idea, but I would braze a small piece over the hole left in the AV. That is what I do.
For testing purposes I have a piece of monster duct tape covering that holeThe reason I braze a cover over the hole is this: it is normally covered over by the choke linkage. Removing the linkage leaves a hole for air flow, which I thought may create a bog. I hope in a few days to have some pics of the discharge tube mods, which I will post.
Yes. We were pulling alot of vacuum during the tests. I believe the suction was just drawing fuel past the check valve. We first put a spring on top of the check valve which stopped it but we lost the squirt function. So later I bought some CS squirters which fixed everything.
Competition Series. They are different"CS squirter" ?
Interesting, Ive got a CS TQ on the shelf, have to check.Competition Series. They are different
They have an open area which acts as a vacuum breakInteresting, Ive got a CS TQ on the shelf, have to check.